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Engine Notes Compiled by George Coles for the Club Journal July 2009 The
rally season is now in full swing and, so far, we are enjoying good
weather. Kelsall, at last, enjoyed a fine, dry weekend. At that event I
was pleased to see a fine new engine that has arrived in the Cheshire
area. This is the Fowler single cylinder agricultural engine No. 8635
“Black Jack”, built in 1899. It was purchased recently by John Paulson
from Helsby. This engine was offered for sale in Cheffins auction earlier
this year but did not reach its reserve price. Eric
Marshall tells me that work on his engine is almost complete. The new
boiler barrel has been fitted by Howard Bros. in Derbyshire, and the
engine fully reassembled. They have steamed the engine and given it a
trial run. It is now to be repainted, so it will be the late autumn by the
time he gets it back. Peter Walker and Diane Carney have now got their “Tarmac” S6 Sentinel back together again. The boiler outer shell has been renewed. They have had a trial steaming and everything seems to be okay. It is having a new coal bunker fitted at the time of writing and the cab needs to be re-fitted. They hope to be back in action by the end of July. February 2009 My
Clayton is currently partly dismantled at Johnson’s of Banks for a new
tender to be fitted. It was low-loaded down there on Boxing Day afternoon
following the Tom Barlow Run. During dismantling it was discovered that
one of the planet wheels on the differential was running without an axle!
As there is no way the axle could escape it must have been running this
way since the last time the differential was dismantled. That was thirteen
years ago! I am having a new chimney base cast for the Clayton as the old
one is in a very fragile state and had done well to last out the season.
Fortunately David Ragsdale has a pattern for a Clayton chimney base so I
have been saved the cost of getting a pattern made. I am expecting to take
delivery of this any time. Alan Porter tells me that the crank shaft of his Burrell Roller No. 3535 has been successfully repaired with the assistance of David Lomas. It has been refitted at Banks and has been tried in steam. It appears to run okay, but there is still a bit of a problem with one of the bearings. Richard Fairhurst tells me that he has finally got the firebox removed from his Fowler Roller. This has confirmed that the firebox crown was seriously thin in places. David McNamee confirms that there will be another event at the Hark To Bounty, Slaidburn this year on June 13th and 14th. There is a new event this year at Harrison’s Leisure, Banks, near Southport on 18th to 19th April. Several local engine owners are involved in its promotion. I am hoping that my own engine will be back in action again by then so that I can attend. 26 years ago, when May Day Steam started, I remember Bill Briggs declaring “You must be b...... mad running a rally at this time of year”. April is very early for an outdoor event. I wish them well! November 2008 We
are nearing the end of another poor rally season. For only the second time
in 41 seasons of rallying I have had a rally abandoned two days before the
event. I had spent the previous Saturday and Sunday steaming my Clayton
all the way across Cheshire from Chelford to Malpas, burning coal which
has cost me over £100. However, of Thursday, the inevitable phone call
came. The field was under water with more rain forecast. The only bonus
was that the chimney had not fallen off during the journey! On an earlier
journey from Kelsall to Tabley House the chimney had developed a wobble.
On examining it on arrival at Tabley, there was a long crack around one
side of the chimney base. After the rally it was dismantled and found to
have another crack on the opposite side. Fortunately George Hudson at
Banks was able to weld the three parts back together, but it remains in a
very fragile state and will have to be replaced. Does anyone know the
whereabouts of a pattern for a Clayton & Shuttleworth Chimney base? The
Tender of my Clayton is now completely “shot”. It consists of much
fibreglass and concrete and very little metal! After the Boxing Day run
the engine will be going over to Banks for John Johnson to fit a new one. Poor
Alan Porter’s problems continue. While steaming to Astle Park the
crankshaft on his Burrell Roller fell apart. It was a previous repair that
had failed again. It has been low-loaded to Banks and, at the time of
writing, as decision is awaited on the best way to effectively repair it. At
the Acton Bridge Stream Party a surprise arrival by low-loader was unique
engine recently purchased by Max Cowap of Bartington. This is the John
Collings No.2 Tractor. He only built three engines, all for his own use,
in a workshop in the grounds of Bacton Hall, Norfolk. The engines were all
unusual and to his own design. Most of the larger parts, boiler, castings,
etc. were all bought in. No.2 is the only survivor and is a Tractor which
was used for general farm work, direct ploughing, reaping, etc. on his
estate. It is a tandem compound with very lightly constructed wheels. The
boiler worked at 250 psi but is in a very poor state and will need
extensive repairs. Following John Collings death in 1950, the engine was
sold and from 1954 was owned by Ronald H Clark, the well known author of
several books on traction engines. It was in working order at that time
and he took it to early rallies in the Norfolk area. It has recently been
owned by Richard Parrott but has been disused for many years Another engine at the Steam Party which I had not seen before was the Foster Traction Engine No.3610, an old single cylinder engine with the front axle set back under the boiler. It was purchased about two years ago by R. Prideaux of Heskin, Chorley but has recently been with Will Woodward. February 2008 At
least two local engines have been active throughout the winter. I came
home from Manchester on the last tram to Humphrey Park one Saturday, about
2 weeks ago. When I got off the tram at 11.30pm Lee Fisk had his Fowler
Roller No. 16078 ticking over in the back garden. The following day he was
seen having a run through Urmston to the local pubs. He was in the company
of Richard Metcalfe on the Clayton and Shuttleworth Traction Engine No.
48232, which he inherited from his father last year. He is now working for
Ian Riley at Bury and is living in the Stretford area. He moved the
Clayton from Macclesfield to Stretford a few weeks ago. Richard
Fairhurst has removed the tubes from Fowler Roller No. 16436. On examining
the firebox he has decided it will not last the life of another set of
tubes, so he will be replacing the firebox. Eric
Marshall is also in the process of re-tubing his Ransom Traction Engine
No. 35247. I gather that it may also require repair or replacement of the
smokebox and front tubeplate. Currently I have the crankshaft out of my Clayton and the flywheel removed in order to get at the main drive pinion. It has been rocking on its keys for some time so it will require new keys making and fitting. July 2007 There
was very little of note to report at the present time, until today! Alan
Porter has completed the re-lagging and cladding of his Burrell Roller and
it is now back in full running order. Eric
Marshall tells me that his Ransoms Traction Engine No.35247 requires
re-tubing and hydraulic test but that he and his son-in-law are too busy
at the moment so the engine is unlikely to be out this year. Rob
Houghton has some concerns over the crank-shaft wobble on his Aveling
Tractor. There is too much end float which is causing the bearings to open
up. He is trying to nurse it along to the end of the season before he
sorts it out. Today
we were taking my Clayton to the Budworth Steam Party. All went well until
a short downhill section just past High Leigh Garden Centre. When Malcolm
Hartley, who was driving, brought the reversing lever back to retard the
engine, there was a loud banging sound from within the cylinder. The
vibration was causing small jets of steam to be emitted from the safety
valves and the Lucy Ashton nameplate came loose and fell off! After
stopping the engine on the brake, and putting it out of gear, it was
apparent that something was loose inside the cylinder. On removing the
cylinder end cover, it was soon clear that most of the piston was no
longer attached to the rod. Luckily there was no damage to the cylinder
block. We
had nothing with us to remove the large nut which holds the piston on to
the rod, so I had to head off home to pick up the large stilsons, crowbars
and anything which might be needed. I also brought the old piston which we
had replaced last winter. Meanwhile
Malcolm and Ben had removed the little end pin and the securing pin on the
piston rod nut. We soon had the nut removed when I returned and we could
then clearly see that the central boss of the piston was still hard on the
taper of the rod, but the main disc had fractured off and was at the
bottom end of the cylinder. I
went down to “The Lock” to see if any of the enginemen there had a
suitable puller. Julian Stafford had just the right tool at home and we
duly collected it. The old piston had two drilled holes in it which had
been used to pull it off the taper on the rod. While at Julian’s these
were plugged up with some suitable threaded bar, with Clive Hearsey’s
assistance. They were riveted over and locked in using some fine wire used
for securing aircraft bolts. On
return to the engine, the puller soon removed the central boss and the
rest of the piston was blown out with a blast of steam. The piston rings
were transferred to the old piston which was then fitted to the piston
rod. After refitting the cylinder end cover and little end pin, the engine
was found to tick over quite smoothly. So we were off again and arrived at
the steam party about four hours later than expected. So
now it is the inquest. What caused the failure? Was it a design fault? Was
it a poor casting? Did most of the fracture occur when the engine primed
very badly whilst leaving John Heselwood’s premises on its first trip?
Perhaps it was a combination of these. The jury is out! Hopefully the old piston will keep us going until the end of the season. February 2007 I
have no changes of ownership to report since my last notes. Most engines
are now undergoing winter maintenance and, in the case of my Clayton, we
are looking at the cylinder this year. I had expected to have to re-bore
it, as I knew the piston was a poor fit. When dismantled and examined the
bore proved to be smooth and parallel, within a few ‘thou’. The piston
rod has been skimmed and new neck bushes made. At the time of writing a
new piston has just been cast and new piston rings are in hand. Neil
Carney has also manufactured new rods and gland bushes for the regulator
valve. Also in hand is overhauling of the injector clack valve and
non-return valve along with renewal of some pipe-work. December 2006 I am indebted to Alan Porter for information on some recent engine movements.
August 2006 Alan Porter tells me that he has finally got to the bottom of the motion problems on his Burrell Roller No.3535. About 20 years ago he suffered a broken crankshaft which was successfully repaired. He has now discovered that the repair has failed and will have to be done again. March 2006 Work on the boiler of Alan Porter’s Burrell Roller No. 3535 is now complete. It has passed its boiler test and is now back on the road for the 2006 season.
Back to Index page All images copyright Rick Fairhurst unless otherwise stated. Email RichardFairhurst@lancashiretec.co.uk
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